Both, with rather disappointing results. The track day was a bust with only one run at the end of the day. I had just fuel injected the car and was running with a quarter tank. On launch the fuel sloshed back and the pump sucked air. Ran a flat 13.0 with the car bucking down to the 1/8th mark until I pulled my foot out of it. Chassis dyno put down 410 peak HP at the wheels with a not so great torque curve. What I think is going on is its driving through the converter. The converter that is in it was spec'd for a stock stroke 360.
Got a few bugs to work out still. I was having a new baffled fuel tank made for the car, but the shop has been radio silent for the last two months. I need to give them a call.